In the meantime I found a couple of things on the RG, a hairline crack in the clutch cover and a hairline crack in the no. 2 carb float bowl! The rear cylinders and pistons look good (the guys told me one cylinder was smoking quite a lot). And it started up no probs, am looking forward to testing the new ignition curve. I also checked to see if the exhaust valves were working and they are. I fixed the clutch cas with JB weld and found a perfect float bowl on an old carb, still put some JB weld on the cracked float bowl just as a spare!
This blog has changed more to be about the bikes in my garage than racing, but hey, I will still be using the RD 350 YPVS and the RG500 on track!
Thursday, 19 December 2019
Ducati gone
In the meantime I found a couple of things on the RG, a hairline crack in the clutch cover and a hairline crack in the no. 2 carb float bowl! The rear cylinders and pistons look good (the guys told me one cylinder was smoking quite a lot). And it started up no probs, am looking forward to testing the new ignition curve. I also checked to see if the exhaust valves were working and they are. I fixed the clutch cas with JB weld and found a perfect float bowl on an old carb, still put some JB weld on the cracked float bowl just as a spare!
Wednesday, 11 December 2019
Brake adaptors for the 350
The second most difficult part is to ensure the bolt holes are exactly in the right place, if they are more than a 10th out it won't work smoothly!
Well it took more than 3 attempts to get it right! The first time I tried it I only had the fork leg and calipers - no relation with the disk and wheel. The second time the disk to pad relation was still a little out.
First attempt |
I worked this through with templates however the cardboard cutouts only go so far... You can't get good accuracy with a cardboard template!
The third time lucky! I will fit them tomorrow and then clean up the ally, only then will we really know!
Thursday, 28 November 2019
Tuesday, 5 November 2019
RG500 Ales feedback
Monday, 1 July 2019
T140 primary chain
So in order to get a better look and measure the chain I needed to remove it.
The the stator and clutch need to come off at the same time to get access. I used metric sockets to unscrew both the alternator (rotor) and the clutch centre nut after having remved the pressure plate and clutch plates, I used my home made clutch blocker and my rattle gun to remove both - no issues.
With the chain completely loose, there was play in both the clutch basket and the rotor... not normal me things. Anyway when you remove the clutch hub the rollers that form the bearing between the hub and backet fall out - there are 20! A part from a little marking on the basket grooves there was nothing untoward. So clean everything up and reassemble.
The chain measured out to be 84 links with a length of 15.75" for half length therfore 31.5 total length, which gives a pitch of 3/8" which is exactly right so the chain has not stretched at all!
Friday, 28 June 2019
Tuesday, 25 June 2019
Daytona in Italy!
What happened was a tool had vibrated forward from under the passenger seat and shorted out the battery, luckily every thing seems to have been saved by a fuse, however the battery was flat so no way even to limp home. I got the bike back today and swapped out the 30amp fuse from the reg/rec and charged the battery up and all was well. The connectors from the stator to the reg/rec had got significantly hot so I renewed them at the same time. Connected up the PC and cleared all the ECU errors and away it went! Phew I thought that was going to cost me at least a new battery! I tested out the diode bridge on the rectifier and the resistance and AC output of the alternator which were all good, just lucky I guess could have been a lot worse!
Monday, 24 June 2019
FZR jetting
Just a quick note to document the change in the FZR after upping the jets to 122.5 and replacing the float bowl gaskets, also changing one of the float assemblies, as it was very loose. Anyway feedback is that there is a vaste improvement in pickup at medium throttle, and although at really high revs it is still buzzy, it is miles better, I could maybe try a half size up - 125 again but it is good enough!
The T140 was making significant noise from the primary chain case so took it apart to find that the adjuster threads were stripped so no matter how much I adjusted it it never held the adjustment! The new one had a slightly larger diameter, so that went into the lathe to trim it down, but it is still sticking at some point and I haven't got to the bottom of it yet!
Thursday, 13 June 2019
Thursday, 6 June 2019
Daytona clutch gasket and FZR jetting
As customer bikes are slow I thought I would have a look at the FZR600 carbs and petrol leak, the leak was dealt with quickly as the petrol tap needed tweaking up, I decided to take a look at the carbs as something isn't quite right. I removed the carbs and proceeded to dismantle, nothing really to report so should I up the mains a tad....? They are 120's so I need to see who can do me some 125's..... Maybe.. I used my new ultrasonic cleaner on various bits of the FZR carbs, trying to get any crap off, we will see
Wednesday, 24 April 2019
T140 won't start
The BB ignition replaces the points with a back plate with two hall effect coils on it, a rotor with two magnets fixed to it is fixed to the crank shaft end, and this generates signals which go to the black box which fires both coils at the same time (wasted spark), although I get a spark at the plugs thought I would take a look anyway!
If you remove the black/white wire and the brown/white wire and rub them together you should see a spark at the plugs - check!
If you move a magnet across the coils you should excite them and generate a spark - check except I had to touch the coils with the magnet to get them to fire!
I used a screwdriver to test the magnets on the rotor, and there didn't seem to be any magnetic power at all, so I removed the stator plate and the rotor and effectively very little magnetic power from the magnets! Strange it says on the Boyer site that the magnets should just about support the rotor plate when lifter with steel, mine don't! Maybe this is giving a too weak signal to the hall effect coils and not generating a signal when at speed?
The price of spare parts for the ignition is ridiculous so I am going try re magnetizing the magnets...... we'll see.
Removing the back plate gives access to the small rotor with the magnets screwed onto it. |
Tuesday, 16 April 2019
Tuesday, 9 April 2019
Daytona
You can remove the throttle bodies partially to replace the o'rings |
Showing half of the IVAC and throttle bodies |
Anyway, my Daytona has been pinking a lot lately, slightly less on SP98 fuel but still anything pulling a load below 4000 rpm, and it rattles a lot..... Talking to the virtual Triumph world the prognosis is an air leak somewhere. Either the IVAC hoses are cracked (this is a typical problem) or somewhere in the admission there is a leak.
Anyway planning a bigish trip so I wanted to get it sorted. So I stripped down the throttle bodies, and I have the o'rings on order.
In the mean time a couple of things to note, there was quite bit of oil droplets in the airbox, which is unusual never seen this before, we are not talking masses but more than usual.
The IVAC hose end pieces are cracked (at least two of them), so this maybe the problem, however am going to change the o'rings as they are ordered and are cheap anyway.
On a different subject I have now wired my USB charger port back to the battery, so I now have a readout of the battery voltage (a plus) but on the minus side the charge is on the whole time (a minus), it doesn't draw much without anything connected but enough to flatten the battery after about 5 days. Temporarily I am unplugging one of the spade connectors when the bike is parked up! What is interesting is that the voltmeter reads pretty much what you would expect around 14V when running, whereas when the thing was wired into the light circuit it was measuring between 9-11V - a very significant difference and enough to make the output derisory when on the light circuit!
Thursday, 31 January 2019
Ducati ignition, 888
Anyway, it started up well, although I didn't leave it running long as was in the garage with doors closed! Anyway that's pretty much finished, although I need to road test it!
The horn button on the 888 doesn't work, so I took it apart and it's a simple contact between the push switch and connectors, however the metal insert in the push button was missing along with the spring. I turned up a small insert and glued it in, and then bent a small spring into the right shape and put it all back together, the battery is on charge, so will test later.
Saturday, 26 January 2019
Ducati ignition
The pickups and wiring loom
The Bosch boxes
The resistances
I am trying to wire up the new ignition box using the 12v feed to the coils and the return from each coil, plus the four wires coming from the new pickups.
I wanted to position the ignition box between the coils, but on checking with the supplier he suggested I keep the box well away from the HT side of the circuit. I think I have enough wiring to be able to site the box nearer the battery.
Sunday, 13 January 2019
Triumph Swinging arm bushes
Unfortunately, with the bushes in, it was impossible to insert the hardened steel spacers, I forced a bit but it would wreck the bushing copper to insert completely. After much cogitating, and contacting the guys that sold me the bushes (LP Williams) I decided the only way forward was to remove material from somewhere! Using emery cloth I first cleaned up the inside of the swinging arm tubes, then working slowly I sanded some material off the inside of the bushes, trying every few minutes by inserting the bushes and then trying to fit the spacers, it took me about 10 attempts as I didn't want to have play in the swinging arm!
Eventually managed to get a tight fit and using my tool on the second spacer to pull it in, the spacers have a tendency to displace the bushes and can cover the grease nipple hole so I screwed a screw (metric) into the hole to prevent the bush from moving over the hole, this worked fine although need to make sure it is not proud of the bush otherwise there will be contact with the spacer!