The 350 worked a dream all weekend, Pierre-Luc took her out first thing Satruday morning and bedded in the brakes (new disks and wheels) plus to wear-in the tyres. Pablo had his first go on the track soon after, and really did well, finishing the weekend with a great position on the bike as witnessed by his knee down at the entry to the tripl left at the end of the straight.
This blog has changed more to be about the bikes in my garage than racing, but hey, I will still be using the RD 350 YPVS and the RG500 on track!
Monday, 31 August 2015
Ledenon
The 350 worked a dream all weekend, Pierre-Luc took her out first thing Satruday morning and bedded in the brakes (new disks and wheels) plus to wear-in the tyres. Pablo had his first go on the track soon after, and really did well, finishing the weekend with a great position on the bike as witnessed by his knee down at the entry to the tripl left at the end of the straight.
Wednesday, 19 August 2015
More work
As suspected 2 of the cylinder head studs didn't appreciate all this repeated activity and promptly pulled through. So the risky business of putting in a thread insert in the 2 stud holes was on the agenda. The tricky bit of this is to ensure all the drilling and threading is done vertically and not on the bonk, otherwise the head won't go on. Because of this I decided to use a drill chuck in the milling machine and setup the cylinder flat on the bed of the mill. As you can see from the first photo managed to fix the cylinder solidly to the bed and then drill and tap for the thread insert. I remember paying a bit of money for my thread insert kit, but it has payed for itself time over especially considering I would be out of the game right now if I had to rely on services from a shop!
Anyway the game plan is to try it again tomorrow with a small amount of gasket silicon on the head gasket, and then if that doesn't work swap the gasket again.
More news tomorrow.
Rebuild continues
Monday, 17 August 2015
Engine rebuild Update
with the originals - at least I know they will torque down, even if they disturb the airflow a little.
Anyway, using very light cuts, I was successful at taking some metal off the inside, and eventually getting a free fit on the con-rod. I did the other 2 in the same way, although I made a bodge of Nr. 2 as I cut too deeply and then had to move the cutting tool out so there is a ridge on that one - I hope it won't matter!
The RG is special in that it uses thrust washers to space out the con-rod on the cranshaft in order that it doesn't touch the crank webs, however the washers are in the small end, so the alignment cylinder, piston, conrod, crankshaft is all linked. So me taking adhoc material off the pistons could affect everything - we will see!
Due to Laurent taking material off the head to cut out the impact damage, I had to check the squish values of the front cylinder, The volume of each combustion chamber is 14.2ccs (measured by Laurent), anyway he gave me the tip of assembling the cylinders with the piston rings removed to that it would be quick to get them on and off, which is what I did.
Wednesday, 12 August 2015
Another quick update
I went out with Olly, him on the FZR 600 and me on the Duke, the FZR has stopped leaking oil from the valve cover, so I think I was probably seeing oil dripping from earlier attempts and leaks, so all is well, except Olly said the head still shakes when you let the bars go. I need to check the tightness of the new headset.
I received my engine parts back from ALCO, with the front cylinders rebored to 57.5mms. Larent left a couple of marks lower down the bore otherwise we would've had to change the cylinder sleeves. So last bore on the front. I also got 2 new pistons for the rear cylinders now at 57.0 mms, he also changed all 4 con-rods and outside bearings on both crankshafts - just over a grand (Euros) if you are interested!
I installed the cranks, and put the crankcase half on, but during tightening/torquing I rounded the head on one of the domed allen head bolts that I purchased specifically for the job from Pro-bolt - not happy! Tried everything to remove the bolt to replace it, but in the end had to drill the head off, and remove the crankcase to remove the rest of the bolt... arghhh. Really pissed off with my (expensive bolts) although the guy at probolts says they are only rated at 16nm torque and I was tightening to 23nms, he told me this was written on the packet - which I haven't checked yet. Anyway replaced with the original bolts which although stick into the airflow, at least they are reliable.
Just in the process of putting my pistons in!
More news as soon as it's together - supposed to be going to Ledenon in 2 weeks time, to run it in!
Speak soon.